43k
didn't look bad - the age was the major motivation - sitting as much as it has leads to varnish - this was further indicated by the failure on the bleed down test - it is supposed to hold 2 bar of pressure at 20 minutes - didn't get close
injector #1 before 287cc after 291cc
injector #2 before 284cc after 290cc
injector #3 before 271cc after 289cc
injector #4 before 281cc after 290cc
looks like #3 was the goofy one causing me the "problem"
good to go now - should run very nicely with these, a new hotter coil, 8mm wires, rotor, cap, O2 sensor, and another set of the iridium plugs
installing A/F guage at the same time, so i can dial mixture in according to altitude
94 Midnight Metallic Blue Cab Porsche 968 w/deviating cashmere/black interior and WAY too many mods to list - thanks to eric for creating
www.968forums.com
"It isn't nearly as expensive to do it right as it is to do it wrong."